(model link: https://makerworld.com/en/models/2798526-the-double-ring-carousel-motorized#profileId-3112952)
The Engineering Behind the Double Ring Motorized Carousel
When MakerWorld announced the Rechargeable Power Kit Challenge, I knew exactly what I wanted to build: a classic, motorized carousel.
The inspiration sparked from a cardboard prototype I built recently, which used three gears to drive two rings in opposite directions while creating a galloping motion for the horses. With that mechanical concept already in my head, I dove straight into CAD the moment my power kit arrived.


Nailing the Base & Gear Mechanics
To ensure perfect fitment, I imported the official 3D models of the electronics directly into my workspace. This allowed me to map out the tolerances precisely, and the massive base piece actually succeeded on its very first test print!

The internal mechanisms, however, required some serious iteration:
- Tolerance Tweaks: My initial 0.15mm gear gap caused catching when the Z-seams aligned. Opening that gap to 0.2mm resulted in a smoother rotation.
- Gear Redesign: During early testing, I noticed the gears were binding. My solution was adding a secondary layer to the central gears to prevent direct friction between specific components, which instantly freed up the movement.

The Big Problem: Weight vs. The N20 Motor
As I moved up to the canopy, I hit a massive engineering roadblock. The upper assembly was simply too heavy (around 264 grams) for the N20 Worm Gear Motor. Since the challenge requires using the provided kit, brute-forcing it with a bigger motor simply wasn't an option.

I knew a thrust bearing would absorb the downward load, letting the motor focus entirely on rotational torque. When I couldn't find a Maker's Supply bearing large enough to fit my existing geometry, I decided to engineer my own. By printing a custom track and dropping in ten 6mm Stainless Steel Balls (FA001), I created a “frictionless” base that carried the canopy's weight effortlessly.
The Hard Choice: Form vs. Function
With the main body spinning beautifully, I faced one final hurdle. The moment I placed the horses onto their wavy tracks, the motor stalled out. It just couldn't overcome the combined friction and the vertical lift required to push the horses up the slope.
I tried everything: lubricating the tracks, widening tolerances, and printing at the absolute lowest layer heights. When nothing worked, I had to make a tough decision. Rather than delivering a stuttering, unreliable model, I scrapped the vertical motion and locked the horses in place.
1: Only wavy track
2: Wavy track and bearing
3 (Final Version): Only bearing
