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Bright3D
@Bright03_3D
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Bio
My design journey started right after I got a 3D printer for my 12th birthday. As a self-taught maker, I built my foundation mastering Tinkercad and am now diving into Rhino to bring more complex geometries to life. My designs bridge the gap between satisfying print-in-place mechanisms, like marble runs, and advanced hardware-integrated kinetics.
Achievements
MakerWorld Guardian
Active more than 20 days out of last 30 days UTC time
Contest Winner
Won 1 model contest award.
Recent Article
Behind the Scenes: Motorized Double Ring Carousel
GIF
Behind the Scenes: Motorized Double Ring Carousel(model link: https://makerworld.com/en/models/2798526-the-double-ring-carousel-motorized#profileId-3112952)The Engineering Behind the Double Ring Motorized Carousel When MakerWorld announced the Rechargeable Power Kit Challenge, I knew exactly what I wanted to build: a classic, motorized carousel. The inspiration sparked from a cardboard prototype I built recently, which used three gears to drive two rings in opposite directions while creating a galloping motion for the horses. With that mechanical concept already in my head, I dove straight into CAD the moment my power kit arrived. Nailing the Base & Gear Mechanics To ensure perfect fitment, I imported the official 3D models of the electronics directly into my workspace. This allowed me to map out the tolerances precisely, and the massive base piece actually succeeded on its very first test print!The internal mechanisms, however, required some serious iteration: Tolerance Tweaks: My initial 0.15mm gear gap caused catching when the Z-seams aligned. Opening that gap to 0.2mm resulted in a smoother rotation. Gear Redesign: During early testing, I noticed the gears were binding. My solution was adding a secondary layer to the central gears to prevent direct friction between specific components, which instantly freed up the movement.The Big Problem: Weight vs. The N20 Motor As I moved up to the canopy, I hit a massive engineering roadblock. The upper assembly was simply too heavy (around 264 grams) for the N20 Worm Gear Motor. Since the challenge requires using the provided kit, brute-forcing it with a bigger motor simply wasn't an option.I knew a thrust bearing would absorb the downward load, letting the motor focus entirely on rotational torque. When I couldn't find a Maker's Supply bearing large enough to fit my existing geometry, I decided to engineer my own. By printing a custom track and dropping in ten 6mm Stainless Steel Balls (FA001), I created a “frictionless” base that carried the canopy's weight effortlessly. The Hard Choice: Form vs. Function With the main body spinning beautifully, I faced one final hurdle. The moment I placed the horses onto their wavy tracks, the motor stalled out. It just couldn't overcome the combined friction and the vertical lift required to push the horses up the slope. I tried everything: lubricating the tracks, widening tolerances, and printing at the absolute lowest layer heights. When nothing worked, I had to make a tough decision. Rather than delivering a stuttering, unreliable model, I scrapped the vertical motion and locked the horses in place. 1: Only wavy track2: Wavy track and bearing3 (Final Version): Only bearing Engineering is all about problem-solving and compromise. While I had to let go of one feature, it guaranteed a flawless, continuous spin for the final piece. After countless hours of troubleshooting, seeing this carousel light up and spin smoothly on my desk is incredibly rewarding!